In the first study techniques have brought the work to study the Sub procedure carefully. Then, analyze technical questions with 5W1H improvement principles, in cooperation with the ECRS, to reduce losses from the movement. Reduce losses from the wait. As a result, a loss that is inherent in the production process, reduced, or be removed. Performance of the work, the better. Next step has taken the production line balancing techniques used to plan the manpower, or to carve a workforce to work smarter. By the time the average on each of the work phases is defined for continuous operation. Jobs waiting cannot occur. Making the working process to just 6 steps, under the terms of the same number of employees. But the capacity has been increased from the original hourly options options 1,668 880 per hour 87.41 percent, as a result, productivity at the station 4 the Department has 111% value and end Cycle Time 4.27 seconds, results from increased efficiency, making use of the resource costs down so it can reduce operating costs, and decreased cash 242,625 25.65% per month in addition to gathering information from customer complaints, and defective goods report suggests that such updates do not affect the quality of the goods.
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